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View Full Version : Another Worthy Garbage Pick :-D


enRo
04-17-2006, 08:47 PM
http://img117.imageshack.us/img117/4965/dscf00358gi.jpg

Blown Head Gasket. Since my dad practically lives at all home decor stores especially Sears (which this compressor is from), hes gonna get the part ordered :-D . 12-13 gallon tank, 100psi... u can pretty much read what it says on the label. Not too shabby :-D

BonzoHansen
04-17-2006, 08:48 PM
You can probably order the parts online.

Tru2Chevy
04-17-2006, 08:51 PM
That thing must be ancient.

How did you know it only had a blown head gasket?

- Justin

camaro2you
04-17-2006, 08:53 PM
wtf u find the best **** lol

enRo
04-17-2006, 09:00 PM
That thing must be ancient.

How did you know it only had a blown head gasket?

- Justin

No idea. I didnt attempt to fire it up. My dad is a mastermind in the small motors field ... so I went out of the house today without really looking into the problem, came home, and he figured out himself it was the head gasket. Didnt get into too much detail, it was beer:30 for him :-D

Savage_Messiah
04-17-2006, 09:15 PM
schweet

NJSPEEDER
04-17-2006, 09:22 PM
gasket for flat head = phone book cover

why buy when you can make for less than half the price :D

good pick

79CamaroDiva
04-18-2006, 01:14 PM
gasket for flat head = phone book cover

why buy when you can make for less than half the price :D

good pick

less than half the price? what phone books are you buyin? mine come free.....

GP99GT
04-18-2006, 01:17 PM
less than half the price? what phone books are you buyin? mine come free.....

well technically, $0 is less than anything...so it does make sense. though i wouldnt use a phone book cover, but a piece of gasket paper instead

Tru2Chevy
04-18-2006, 02:08 PM
I always used a phone book cover or manilla folder for head gaskets in my 5hp briggs kart motor. Never had an issue with them at all....

- Justin

enRo
04-26-2006, 07:04 PM
Nice update. It was the head gasket... $9 part ... the bolts that hold the motor in needed to be loosened and the motor needed to be shimmied over, because it was slow-building + when the compressor cuts out at 110 and gets back down to 70, the pulley wasnt catching the belt so it would basically sit there and slip until you pushed on the motor. Now it builds 2x faster! The only problem with it now is the valve which is leaking air, which is prolly a $10 part ... then Im gonna strip it down again ... sand the tank, paint it, and its ready for use :-D