Another failed inspection thread
So I failed inspection this morning. I haven't had a chance to look at anything yet so keep that in mind. I am going to start with checking the plugs, wires, cap, rotor, the timing, OHMing out the CTS and going from there. Here are the results from this monring.
Test: Idle, Status: Fail Reading - Standard HC ppm 1846 - 220 CO% 0.58 - 1.20 CO2% 10.1 O2% 6.0 Test: High Idle, Status: Pass Reading - Standard HC ppm 147 - 220 CO% 0.12 - 1.20 CO2% 12.2 O2% 3.3 Needless to say GTA = Fail at the moment Suggestions are welcome |
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or I can fix the problem
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yeah not a good idea since i have to get on a federal installation every day and they actually look at that stuff
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Im good, I'll just fix it
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change the icm thats why my truck didnt pass inspection
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I am goinna start with checking the plugs and stuff and work my way back to the distributor. The ICM did cross my mind. Something has to be a miss for such high numbers
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Start with the basics. Verify the condition of the ignition system.
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what is the idle rpm?
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I have to go next week....'92 bird here....cross your wings, it may get bumpy.
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Possible that the idle is too low?
The HC at low idle might be caused by a missfire, or possibly a leaky injector. |
Car had injectors replaced by the PO who I know very well. I am going to reset minimum idle when I check everything else. Just for peace of mind
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swapped out the plugs and CTS today. gonna go for a long ride to let the ECM re calibrate and then go back for a re-test and see if its any better
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My results looked similar on my formula..bearings on my crank are bad. That idle sounds way low..
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I'm sorry but is one to infer that "bad" crank bearings would result in high hydrocarbon readings during an idle test? Just want to clear things up.
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Uh, no.
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Failed again. HC ppm is down to 424 on low idle. Going to change the wires and check timing and bring it back again. Didn't change the wires initially because I inspected them and they looked good but not I'm going to change them hopefully on my lunch break if I can squeeze my paw down enough to grab the plug wires from on top instead of underneath....its a long shot I know
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It's possible that throttle body is dirty or the plate is closed too far. Check that out. If it's dirty or closed too far the PCM will add timing to compensate once it maxes out the IAC, which will skew your HC readings.
Edit: Also check to see if your IAC is clogged/dirty. |
I adjusted minimum idle up 100 RPM and changed the wires tonight. gonna go back in the morning, if it doesn't pass this time I am going to have to check and adjust timing
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make sure your timing is at factory spec. that will impact low rpm emissions.
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When was the oil last changed?
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