Compression was good. I did a 4 puff test which GM suggested. I was unable to see the gauge until I stopped the test. A GM tech on another forum said he has seen this twice in the past. One was a bad PCM to ground wire. The other was a bent/broken valve spring. Compression can still be good with a bent/broken valve spring per what he said. It is just something I would notice on the 1st puff, not after 4. Of course he tells me that now.
I appreciate the offer! Harrison is approx. 2 hours+ away from me. My zip is 19380. That's a long drive in this car with the way it is currently running.
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-Rick (Photographer)
- 2001 Trans AM WS6 - M6, ORY, Borla catback, etc.
- 1998 Trans Am - M6, functional Ram Air hood, Flowmaster, 3" QTP E-cutout, ORY, K&N FIPK, 3.42's, LSD, Hella 60mm Projectors, 4300K HID's & more.
- 2003 VW Golf TDI - Turbo diesel @ 50 MPG highway
- 1998 Jeep Grand Cherokee 5.9L(ZJ) - 4.75" lift, 32" MTZ's, armor, etc.
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